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Feb 16, 2018 18:49:39 GMT
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Hehe, I recall stalling my first car, a 1973 Fiat 126 immediately following a new clutch being fitted - at around just 18,000 miles (my dear old grandparents must have ridden the clutch, I guess...)
Been through all that exhaust flange leakage malarkey on my 1970 Minor Traveller too; original clamps were cheap pressed steel items that rapidly become slack - a proper 2-piece cast item with brass nuts is far superior.
Ideally, fitting an LCB-type 'bunch of bananas' exhaust manifold to take the gasses right underneath the car with no joints in the engine bay is the best solution.
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vulgalour
Club Retro Rides Member
Posts: 7,270
Club RR Member Number: 146
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Took the Princess to the local trusted exhaust place and the one guy there that knows his old stuff had a look. The conversation was mostly "You're on your own with that one!", which was entirely fair. Basically, the problems we're having getting it to seal is normal for this kind of exhaust and if it's a poor quality exhaust to begin with, my experience of it blowing eventually is also normal. This is from someone that has fettled with BL exhausts since they were much newer than mine is and still fettles with exhausts now for a living. His advice was not to waste the cash on getting them to try and seal the exhaust as they'd be likely to have the same success/failure rate as us anyway and it'll probably blow again soon after forking out to have it fixed. I appreciate honesty like that, rather than being messed about, and it was reassuring to know that it is actually genuinely a problematic set up rather than us being inept.
We were given some tips on fitting, at least. So far, we've done mostly everything right but actually getting the manifold-to-downpipe join sitting as snug as possible before sealant and clamps is the most important bit. That might sound a bit daft, but given the design it's easy to think you've got it lined up perfectly when it's actually just a bit off, which in turn can cause the issues I've been having.
So, disconnect the blowing join, clean it up, make the flange as perfect as possible and wiggle everything about until it's lined up as close to perfect as possible without the clamps. Then use some paste, tighten the clamps and get the rest of the exhaust secure. It should then seal, or at the worst only blow a tiny little bit.
Ideally, replacing the cast manifold with a suitable custom one-piece banana bunch that goes into a good flexi joint and on into the rest of the system is the best solution. Unfortunately for me, a custom exhaust is out of my budget currently so we just have to do the best with what we've got and do the exhaust when I can afford it.
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CaptainSlog
Part of things
Posts: 510
Club RR Member Number: 180
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Hang in there Vulg, we have all been down the same noisy, awkward, messy, frustrating road with that flange.
Some of the things that Issigononis designed were genius, others, pure curse word. How BL and the others continued with this completely useless design for so many years is beyond me and a good example of why the British motor industry went the way it did.
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glenanderson
Club Retro Rides Member
Posts: 4,326
Club RR Member Number: 64
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Feb 18, 2018 10:30:37 GMT
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Sometimes it’s worth dismantling the next joint, and dropping the rear part out of the way, so you can concentrate on getting the downpipe/manifold flange exactly right without the other end being held rigid. Once you’ve got the front joint on square, tight and leak free you can force the rear part of the pipe into place to suit the next section.
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My worst worry about dying is my wife selling my stuff for what I told her it cost...
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Feb 18, 2018 12:31:12 GMT
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What Glen said. Much easier to manipulate a smaller section than the whole system.
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Feb 18, 2018 16:14:19 GMT
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We used a different approach with the reoccurring ones by chopping 150mm out of the downpipe just above the exhaust bend at the base of the bulkhead / floor pan and then sleeved it with a length of steel flex exhaust which was brazed on at each end - this would give the flexibility to the downpipe to obtain the correct fit and continue to offer flexibility throughout the use of the vehicle - no matter how good the engine mountings were you will always get some torque reaction / rotation with the BLMC transverse engine range has the clutch is released and the wheels / tyres transfer the grip to the road surface - I think on some models this flex joint in the exhaust was original equipment (certainly was on my late stepfathers Wolseley 6)
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Feb 18, 2018 17:12:54 GMT
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I ‘think’ * thats how my dads was sorted,a combination of new mount and a flexi piece ....
* it was a very long time ago .......
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Feb 18, 2018 17:23:42 GMT
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I had a similar issue with one of my many Minis back in the 90s. The downpipe to manifold would not seal no matter what was done to it. I swapped the manifold for an identical one from my mate's garage and the problem was solved. Sometimes there's just a tiny problem that you can't see. It doesn't help that it's such a god-awful design. If you have a spare manifold then try that. It can't be any worse. Hope you get it sorted.
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Feb 18, 2018 17:34:27 GMT
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Feb 18, 2018 17:51:39 GMT
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Good idea but it's not that simple the manifold & the downpipe have external flanges that mate with each other and are then retained by a clamp - some models had a sealing ring between the two flanges and then the clamp - hence its not your normal flat face's that you are sealing a gasket against
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Feb 18, 2018 20:37:24 GMT
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I agree with grumpy - I would cut the exhaust lower down & fit a flexi pipe and I'd just weld the manifold & upper pipe together.
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vulgalour
Club Retro Rides Member
Posts: 7,270
Club RR Member Number: 146
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Feb 19, 2018 19:21:46 GMT
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When cash is more free flowing, custom exhaust is what I'm doing. Today I have learned my exhaust is very much not fit for purpose. --- Exhaust then I suppose today. Drive over in the Princess as normal, nothing amiss beyond the exhaust noise and I find the throttle getting gradually stiffer until I'm approaching lights and suddenly the throttle jams completely. Fortunately I was next to a bus stop so could throw the car into neutral to stop it running away and turn it off to coast to a stop. Hazards on, bonnet up, have a look. Somehow, it was earthing through the throttle cable again even though all systems were normal. I had noticed a dip in the ammeter with the headlights on, much the same as yesterday, but it was stable so just assumed the battery was a little low from lack of use. I let everything cool down and the throttle returned to normal, I then carried on to the unit with the headlights off, which I don't like doing on a drizzly day, but it was less than a mile of the journey to go and nothing untoward happened. Wasn't particularly thrilled about this so the first job was to investigate the earth issue and we thought we'd resolved it when we noticed the headlight earth point was a bit dirty. Made a brand new earth point which improved matters, but after a while the throttle cable started to warm up again if the headlights were on (and only the headlights), so I need to find out what's going on with that. At the moment the earth points check out fine and there's nothing obvious, all I can say for certain is that something on the headlight circuit isn't routing electricity as it should and further investigation is required. Exhaust next then, since I didn't want to chase electricals until that was sorted. Air filter box, carburettor and heat shield off first for access. I never disconnect the cables going to the carburettor because the end of the cables always fray and I can never get them back in again, so I always make use of the flat bits of the engine bay to keep the carburettor out of the way and still connected. Unconventional, perhaps, but saves me the expense and hassle of fitting a new pair of cables every time the carburettor comes off... which has been a lot lately. 20180219-01 by Angyl Roper, on Flickr Mike and I wanted to make the exhaust components that were leaking as clean as possible so we opted to remove the manifold rather than dropping the exhaust this time. This was also a consideration after folks on my various threads suggested the manifold casting can have flaws that cause issues with sealing, so we could deal with that too if it turned out to be the case. The exhaust downpipe flanges didn't look too bad, with the exception of some exhaust paste to remove of course, so that was something. 20180219-02 by Angyl Roper, on Flickr 20180219-03 by Angyl Roper, on Flickr With everything cleaned up, which took forever, we aligned the manifold to the downpipes and immediately a problem became apparent. We moved things around a fair bit to double check and played with the clamps and dry fitting to be sure, but it looks like one of the downpipes is at the wrong angle and if you bent it to be at the correct angle, it wouldn't sit in the correct place to meet the manifold. This is probably the root cause of the exhaust blow and only a replacement exhaust is going to solve that. I was therefore okay to accept the exhaust will blow when reassembled, I cannot do anything about this at the moment. 20180219-04 by Angyl Roper, on Flickr After fiddling about with the clamps and the jack and the exhaust, we got a better fit than the above photograph by sort of wiggling the manifold down onto the pipe with me bracing various pieces while Mike got the clamp tightened up with a little exhaust paste. Then the chore of refitting the manifold while it was attached to the exhaust, which is about as difficult as you can imagine since it goes on with bolts rather than sitting on studs and there's a gasket to fit at the same time, so you need about 6 hands attached to two arms. It was like playing Twister, just a whole lot less fun. With it all bolted up the extras were reattached so the car could be started and here's an idea of the access available to you if you don't remove everything first. 20180219-05 by Angyl Roper, on Flickr 20180219-06 by Angyl Roper, on Flickr The end result, on starting the car up, was that the driver's side clamp has sealed perfectly. The passenger side one has a little bit of a blow, it's tolerable and should go through an MoT at least and will likely quieten down a bit once the car has been through a few hot/cold cycles. Partial success at least. Annoyingly the carburettor then decided it was just going to pour fuel out of the overflow while idling and didn't want to respond to any sort of attention and the headlights are still trying to earth through the throttle cable. So the Princess has been left in the sin bin at the unit for a bit to think about what its done while I try and find the next bit of free time to go through the electrical issues with Mike. Carburettor is probably just a stuck inside component, low oil in the dashpot or simply because SU. I hate problems like these because they take ages to find and sometimes, even worse, mysteriously fix themselves.
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Rich
Club Retro Rides Member
Posts: 6,320
Club RR Member Number: 160
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Feb 19, 2018 19:27:21 GMT
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Sounds like the body to battery earth lead is bad, the earth path tracing through the car, throttle cable, engine block and back to the battery via the motor earth. Although that theory only stands if the motor earth goes straight to the battery. How odd.
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vulgalour
Club Retro Rides Member
Posts: 7,270
Club RR Member Number: 146
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Feb 19, 2018 19:51:56 GMT
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My first port of call, once I figured out what it was doing, was to check the main earth strap and it's fully secure at all points and perfectly fine with no sign of damage, heat or sparks when you start the car, nothing is loose. It's a very odd fault and I'm expecting it to be something weird like I was getting when the original cigarette lighter had got loose and was shorting out causing weird lights issues.
It could be related to the duff bulbs in the dashboard so that's going to be the first port of call. It's odd that it would do this today, but not the last time I took the car out.
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Feb 19, 2018 19:59:20 GMT
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Earth strap on engine. Add a second one even if it looks ok it might be poor inside.
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vulgalour
Club Retro Rides Member
Posts: 7,270
Club RR Member Number: 146
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Feb 19, 2018 20:11:03 GMT
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It doesn't really have an inside, it's one of those flat braided types. Apart from seeing if it's hot or frayed, I'm not really sure what you'd check on that sort. A second earth strap I can do, I have a couple of spare cable-type ones which might be better?
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Feb 19, 2018 20:15:29 GMT
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Clamp a jump lead from neg on battery to block see if anything changes.
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vulgalour
Club Retro Rides Member
Posts: 7,270
Club RR Member Number: 146
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Feb 19, 2018 20:17:51 GMT
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Why didn't we think of that? That's a brilliant idea for fault finding!
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Feb 19, 2018 20:21:59 GMT
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Flat braided is old and were never very good. Put a decent one on, or if quality is suspect put both spare ones on.
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Feb 19, 2018 20:26:43 GMT
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Easy way to check earth resistance.Put voltmeter between engine and body.Disconnect coil and get someone to crank engine for 4 or 5 seconds.Anything above o.5 volt and earth path is compromised.
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